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Restoration diary

Reports of restoration work on 50029 and 50030.

Announcement of working party dates and details of restoration work carried out at working parties.

Work party report 17 September 2023

Work party report 17 September 2023
Dave Rolfe, Richard Wade, Jay Hirst, Mark Burrows and I were on site today. Richard carried on checking the battery isolation switch and shore supply and battery charge wiring. Jay and I attempted to fit the upper internal panel that goes above the change end switch in No.1 cab, but most of the mounting holes didn't line up, so we looked ...
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Work party report 3rd September 2023

​Dave Rolfe, Carl and Sofy Looker, Richard Dale and I were on site today. Dave was removing pipework from the spare cab (formerly of 50037 Illustrious and purchased for this very reason), Carl and Sofy rubbed down and undercoated all four cabsides on 50030, then removed some cab handrails to de-rust and prime the difficult-...
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Work party report 13th August 2023

Mark Burrows, Dave Rolfe and I were on site today. Mark brought back the 16 overhauled fuel pumps, and they were placed in store for now. Dave started pressure-testing the two air engines that operate the rad fan shutters on either side of the radiator compartment now replacement covers have been fabricated for the EP valves, as the originals ...
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Work party report 6th August 2023

Work party report 6th August 2023
​Dave Rolfe, Richard Dale, Jay Hirst and I were on site yesterday. Richard finally finished drilling and tapping the fixing holes for the mounting plate for the change-end switch in No.1 cab, a difficult job because most of the holes are either at floor level, or right next to structural supports for the cab desk and the bulkhead the driver's ...
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Work party report 23rd July 2023

Work party report 23rd July 2023
​Dave Rolfe, Mark Burrows, Richard Wade, Jay Hirst and I were on site today. After barring round the power unit and oiling the turbos, Dave and Mark began investigating the broken air pipes I'd discovered under the floor in No.1 cab, finding virtually all those that dive through the plating under the cab floor had corroded away, on both t...
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